|  | Home > Maintenance & Mods (L322) > Suspension fault and blowing every 10 seconds | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | iid seems to permanently show 100% open for the exhaust valve - the other body’s and solenoids etc say 0% Current stable:
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|  24th Jun 2025 7:49am | 
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| dingg1 Member Since: 29 Jun 2013 Location: PORTUGAL Posts: 1422    | Check height sensor readings for an anomaly? | ||
|  24th Jun 2025 8:50am | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | Be been driving with that screen up permanently to check it doesn’t suddenly drop - all looks above board Current stable:
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|  24th Jun 2025 9:54am | 
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| dingg1 Member Since: 29 Jun 2013 Location: PORTUGAL Posts: 1422    | Check them with iid tool or similar, what shows on screen may not be a true picture of the state of things, can't think of anything else tbh
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|  24th Jun 2025 12:34pm | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | Awesome did you change them all? Glad it was the same fault Current stable:
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|  24th Jun 2025 7:27pm | 
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| dingg1 Member Since: 29 Jun 2013 Location: PORTUGAL Posts: 1422    | Just stripped and cleaned them , all seals looked good ,no dirt or grime evident, but its done the job.
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|  25th Jun 2025 11:22am | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | Awesome….
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|  25th Jun 2025 5:09pm | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | A small update… I was convinced that the puff of exhaust would happen from the exhaust or straight from the main pipe feeding to the compressor so I disconnected it… I was wrong… air came out fast for about 3 seconds along with a lot of water droplets… i then took the exhaust solenoid out and it was wet… I check the drier it was bone dry. So i then left the solenoid out and started it a few times to let it blow the wet water out. Then I put it back together and it’s all good now 😃… I am a realist though something is causing moisture in the air to the system and it’s not in the compressor and this will likely happen again until resolved. Any ideas? Current stable:
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|  27th Jun 2025 7:18am | 
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| Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2309      | Just to close this off I ran a full discharge of air through iid tool and reinfected and drove 200 miles yesterday… so far so good. Got a water trap to put inline too Current stable:
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|  29th Jun 2025 9:12am | 
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